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5 Posts
Hello world!
Recently acquired a 2010 Clubman (non-s) with 100k mi and been doing some routine maintenance to keep things rolling along. Unfortunately I hit a snag and would greatly appreciate some advice. What started as a simple weekend valve cover gasket and plug job has turned into more...
Initial issues:
What has been done (in the order completed) :
Status:
I hoped the coil packs had gone bad and replacing them would solve it but no dice. Next thought is to buy another new set of plugs - maybe something is wrong with the new set I just installed? In a perfect world I would have done a complete timing chain/guide replacement while in there but I didn't see anything else broken/out of place other than the upper timing guide. Crazy part is the thing was running almost perfectly before opening it up to do the gasket job.
Thanks for your suggestions!
Tom
Recently acquired a 2010 Clubman (non-s) with 100k mi and been doing some routine maintenance to keep things rolling along. Unfortunately I hit a snag and would greatly appreciate some advice. What started as a simple weekend valve cover gasket and plug job has turned into more...
Initial issues:
- hesitation/pulsation from the engine when its under load/bogged
- small amount of oil in some of the plug shafts
What has been done (in the order completed) :
- Replaced valve cover gasket and o-rings
- Replaced spark plugs
- Replaced upper timing chain guide (bracket was broken off near the studs....a very surprising find!)
- Replaced the coil packs
Status:
- Car starts right up and runs normally
- Seconds later the engine begins to sputter and stalls
- No CEL or codes in the ECU
I hoped the coil packs had gone bad and replacing them would solve it but no dice. Next thought is to buy another new set of plugs - maybe something is wrong with the new set I just installed? In a perfect world I would have done a complete timing chain/guide replacement while in there but I didn't see anything else broken/out of place other than the upper timing guide. Crazy part is the thing was running almost perfectly before opening it up to do the gasket job.
Thanks for your suggestions!
Tom